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1972 F-100 4x4 refurb

bigjohn

Active Member
Well last fall I took this truck in on part trade for another rig I was selling. I really, really didn’t need another project but I have a weak spot for F100 4wd’s. The thing Was fairly solid, except the cab. The roof was extremely rotten. And it hadn’t run in North of a decade. And the distributor and wires were long gone. And there was an engine fire at some point. But it is another side project I can dink and dunk together over time.
It’s a 72 f100, 360 I imagine, 4 speed, with a 205 transfer case instead of the Dana 21 single speed the slightly older f100 4x’s got. The 9” and 44 seem to have the standard 3.50 gears. And it came with those terrible 90’s wheels and super old 33 Wildcat ext’s. Those got replaced with some orange steel wheels and decent 35’s I’m from my parts hoard.
So the first step, after a Good pressure wash, was to pull the hood and install a temporary fuel system and ignition setup. I went moderate in the ignition department with a Jegs brand ready to run distributor and coil. The fuel system was a clicker pump powered by a Milwaukee m12 battery and a boat tank on the passenger bench seat. After lubing and beating on the edelbrock 4bbl it actually fired up and ran ok! But that was short lived. The edelbrock slowly got worse and worse. I eventually swapped on a good Holley 650 double pumper I had on the shelf. I also plumbed a new Carter mechanical fuel pump back in, and moved the boat tank to the bed. There are 3 home built tanks under the bed, and zero I trust. It ran for a bit with the large rear center tank but it lacked fuel flow to do anything but property driving. So back to the boat tank.
A while later I ordered some brake parts and replaced the wheel cylinders, master cylinder, rubber brake hoses and the shoes. This got the brakes functional. While I was in there I cleaned and lightly lubed the hubs to get them functional again. It still needs a new booster but I’ll get there.
The truck came with a really solid but completely stripped cab. Well once the rain came I realized just how little water that original cab kept out. I hadn’t planned on driving in this soon but i had some down time between a few other projects so i snuck it in. The front clip came off and the cab was off over Christmas weekend. Then pressure washed the engine and frame, sanded and por-15’ed the frame from the bed forward.
While the cab was off, I’d scored some free and almost crack free fe exhaust manifolds. The problem was 6 of 8 upper manifold bolts broke. No amount of heat, penetrant, wax, ect would prevent this. I ended up having to torch the bolts out of the upper head holes, clean the holes with a right angle drill I ordered just for this occasion, and run the tap through the holes. With some new remflex gaskets and new donuts, the new manifolds went back on.
At this point it was the monotonous task of stripping everything out of the old can and reinstalling in the new. I went through and cleaned some butt connectors, scotch locks, and extra crap from the cab harness before relooming it and installing it. Every cab plug, wiper assembly, heater box, even the dome light wire had to be swapped. I also por-15 painted under the dash, under the seat and behind where the in cab tank will be reinstalled.

Over the last week the new windshield came in so father in law Jeff came by and we got both the front and rear glass installed. After he left i installed new door seals and reinstalled the doors. They still need lots of adjusting but I’ll get it.

This Friday I went down to Tony’s Ford truck parts and picked up a passenger inner fender and core sport to replace my rotten stuff. That night and Saturday I spent a ton of time degreasing, cleaning and painting them. And today I finally got to start the assembly process. It was time consuming. Fitting, chasing threads, wiggling, moving. But the inner structure is together and the passenger fender is hung.

I’d gone to a swap meet today and scored a 100 amp power master alternator and a new starter relay, all for $45. So I got those installed while I was in there. And was rewarded after getting it all mounted, with a functional ignition switch again! And no audible exhaust leak from the driver seat, although I know the number 1 exhaust port has a small crack

So this is where we’re at today. I need to flip the alternator brackets for a better alternator fit. Adjust the doors. Reinstall the driver fender. Then I can reinstall the grill and radiator. Install the new door sill plates and dome light. Replace the heater hoses. And eventually replace the radiator hoses. And also eventually the steering linkage needs redone.

I should note, the freeze plugs are still shiny and all indications from the cylinder wall cross hatch pattern and super clean rocker areas in the heads, say this engine doesn’t have many miles on a rebuild.

Ok here’s some pictures.

Oh, before the cab swap, I’d parked in front of the barn and set the brake. Well, the return spring was missing from the release lever. I came back out and the truck was gone. It had exited the barn parking apron, hooked around and went in the gully. This could have been far worse. It knocked the bed into the cab but was otherwise none the worse for wear. And of course the cab got swapped anyway.
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Love it. These old Fords are so simple to work on. Also cool that it has a 205 instead of that garbage D21.
Oh and thank you for getting rid of those wheels! :D
I couldn’t agree more. This era is my favorite. Man they were built sturdy. I’ve had the d21 in a few other f100’s and to be honest, I always thought they were neat. With the granny 4 speed you almost never noticed the lack of low range. This one I appreciate the low range much more with the 35’s and presumably 3.50 gears.
A few more things got checked off the list this week after work. I got both doors adjusted. They’re both pretty tweaked, particularly the driver side. I imagine whatever did the long ago poorly repaired roof damage years ago also tweaked the door window frame. But it’s should keep water out and it’s not a restoration job. Just getting an old truck back on the road.

I also got the driver fender installed and a bunch of adjusting on the passenger fender as well. Once all that was fine, I installed my new dome light And lens that came in Monday. Id already fished the wire up inside the a pillar and across so that went easily. Once I hooked up the door switches, it came in, and the door switches are working fine. It’s the little things in life.
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With a sigh of relief, I say, the truck is back To being fairly functional. I’ve been fighting body gaps and fitment issues like crazy. I finally had to gain some perspective. This isn’t a restoration. And many of the components I’m messing with are mystery pieces. I know the cab had damage. Well it turns out so did the driver door. And the front driver side corner. Of, and the hood has a number of issues.
All that to say, the truck is complete again. The cab and core sports are bolted down. Everything is about as bolted as it’ll be. The radiator was a battle. I ended up cutting the upper mounting flange and welding to the lower due to different mounting configuration with the new core support. As were the door sill plates. But dang if she’s not a driver again! The boy and I took the twenty minute 4 low trip around the mossy road loop. Its still crazy to me how nice an fe sounds without Million exhaust manifold leaks. Man it’s running and sounding goods. “Grandpa loud” is overstating the exhaust tone, which I love!
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Sharp looking truck! I wish I still had my '78, but it needed engine work (really lots of other work too) and I didn't need another project.
 
I like that truck!!
I had one very similar. My 1st vehicle. a 1971, F100, 4x4, 360 with np 435, dana 21, and 4.11 gears. Short bed.
Actually it was the same color as yours.
It finally rusted down, so my brother and me made an off road toy out of it. This was about 1985
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And these 2 badges are all that’s left
It was a Sport Custom
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I like that truck!!
I had one very similar. My 1st vehicle. a 1971, F100, 4x4, 360 with np 435, dana 21, and 4.11 gears. Short bed.
Actually it was the same color as yours.
It finally rusted down, so my brother and me made an off road toy out of it. This was about 1985
View attachment 104217
View attachment 104219
And these 2 badges are all that’s left
It was a Sport Custom
View attachment 104220
That is super cool! And a sport custom! Probably no chance it was one of the very few factory bucket seat trucks? Those were sport custom only. And that short wide square body cool as heck too. Thanks for sharing!
 
We’ll work continues on the f100. Not much to do at this point. I’d lengthened the adjusting bracket for the new alternator to get the rear bearing housing away from the head. A longer 47” belt was about perfect for that. Then more dinking with the door adjustments.

I had a thought Dawn on me as well. We were running out of fuel in the first road test drive climbing the hill past my house, using the homemade larger rear tank. When a carb change didn’t fix it, going to a boat tank did. Since then I’ve added a stock style mechanical pump, that was pulling through the electric edelbrock pump. The thought; if the electric pump was wimpy to begin with and pulling from 5’ from the tank, fuel is going to have a weak flow. So last night I pulled the hose off the rear tank and immediately had a flow of residual gas in the tank. So I removed the boat tank from the equation. Plumbed back to the rear tank, and changed to a clear wix filter to monitor, added 4 gallons of fresh 92 clear gas, used a drilled spray paint cap and some air to help prime the system, and she was running again on her own fuel system.

This morning I got after replacing the passenger tire rod end- probably the worst I’ve seen. After roughing in the toe in adjustment, i fired it up and drove up the hill and it was fine. So I added another 4 gallons and drive to our local country store, about 10 minutes away. The brakes are not good. Super spongy pedal and audibly leaky booster. I suspect it’s the wrong bore master. I’m going to try a 1 1/8” master and maybe a non leaky booster.
It’s otherwise a decent driver. I know it needs a few more steering parts and track bar bushings but up to about 45-50 mph, it’s a decent drive.

Here’s a few pictures of two of the three homemade tanks. The driver side saddle tank measures to be 11.9 gallons and the rear main tank is 23 and change. I’m guessing the passenger tank is about the same.
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Oh, a few more side notes.
The alternator, with the newly tight belt is charging at 14.4 volts at idle with lights heater and wiper going. That was just over 13v before, both with the loose belt and the old externally regulated alternator.

Opening the secondaries sounds awesome, but pushes past the clutch. I need to readjust the clutch. But it’s not happy and I see a clutch change in my future.

The passenger exhaust manifold still clicks under load. I really regret not even attempting to braze it. The exhaust is 100 times better, but still annoying.

And last, it needs more tuning. I don’t recall if I ever set the timing with a light. And I know I haven’t touched jets, or even pulled plugs since shes been alive again. Much of the tuning though have to come after some road miles; which are tough to get with the current brakes.
 
No
Nope
It was a bench seat.
I always find myself checking every sport custom bump side I see for bucket seats. I’ve found one so far, Mardi report verified. This is funny because I love the idea of buckets, I Have no interest in them in actuality. My kids would eat me alive, like they did with the 2 seat corvette last year that’s more gone. Gotta have now than 2 seats.
 
Not much new to report this week. The new AMD battery tray came in Wednesday so I installed that. I’d already thread chased the bosses so that was easy enough.
Also the adhesive insulation came in from Amazon. So I got some sheets applied behind the seat where stock fuel tank will eventually reside, and the roof so I can finally start thinking about a headliner.
Otherwise, property driving it is going great. There’s going to be a few fuel filter changes. I should and probably will, pull the bed and remove, clean and line the tanks. Eventually. First priority now is finish the steering and brakes.
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